Friday, June 24, 2011

Easier to Assemble Than an IKEA Bookshelf

When I first started taking this machine apart, I had a slight nagging feeling it would be very difficult to reassemble. I had no idea what I was doing, and therefore took pictures of absolutely everything from multiple angles. As the boiler more or less obstructed everything else interior to the frame, I saved it for inclusion at the end. So, at reassembly, I had a bare black frame and a pile of parts. The boiler, cable, and solenoid mounts I had painted white were the first to reattach to the frame. They were previously riveted on, but I drilled those out and used some screw/nut/washers that I picked up from Home Depot. They snugged in tightly and offered both a removable and aesthetic upgrade to the rivets.

I wanted to see the water level gauge in position, so I attached it next. It used a couple of permanent screw mounts welded to the frame that the washers and nuts tightened against to hold it in place. The next logical part was to add the group heads, which meant it was time to attach the stainless steel front panel to the frame. I made one slight mistake here. For one of the group heads, I had removed the rear threaded double-posts when I did the acid bath soak. The other one was so corroded, I couldn't extract it without damaging the threads, so I just left it in and scrubbed the rust off after it soaked. I didn't realize that one end of the post was slightly longer than the other and that was the end that needed to point out. I mounted it the other way onto the frame which resulted in less post to grip with the nut on the frame side of things, and a slight gap between the group head and the frame on the front side of the machine. After assembling the copper tubing to the group heads, this was less of an issue, and unable to loosen the posts from the group head I just left well enough alone. I added a few copper inlet and outlet pipes to the group heads, and mounted the hot water solenoid assembly on the upper mount.

This was my next mistake which actually occurred much earlier in the project. The assembly attaches by a small bolt that screws into the top of the brass assembly. I over-torqued it and sheared the bolt off inside the assembly. I dutifully went to Home Depot, purchased the smallest Easy-Out bit I could find, drilled out the center of the broken bolt, and promptly broke the higher tensile steel Easy-Out off inside the broken-off bolt. Further attempts to drill it out and re-tap the hole were considered too risky, so I instead drilled 3 additional holes on the mounting bracket, and used zip ties to hold it in place. Inelegant, but effective.

With the group heads securely holding the face plate on, and further bolstered with the inlet and outlet tubes, I incorporated the water inlet tap that mounts under the drip tray and began connecting the tubing and pipes that snake around to the back through the frame cut-outs.The water inlet tap mounts through a couple of holes in the bottom of the frame, but I held off securing it until I had the copper pipes and tubing reconnected. Speaking of tubing, I decided to replace the rubber surgical drain hoses that connected the hot water solenoids at the group heads as well as the drain from the boiler safety valve cap and the water inlet tap. I found it at Home Depot for cheap, but had to use clear vinyl tubing on the group heads since they didn't sell the surgical tubing in a small enough diameter. It may be one of those modifications I'll live to regret, but for now, it looks good and feels snug.

I mounted the pressure gauge and it's cleanly painted mount frame, and continued connecting pipes according to my deconstruction photos. There were a couple of pipe pairs that appeared identical until I tried to connect them to additional pipe connections. After a quick swap, everything was lining up where it should go.
I tried a dry-fit with the boiler in place to make sure all the connections were lining up right and it appeared to be okay. However, once I started tightening down the connections, I discovered the left side group head to boiler lower connection was tightened too far to connect while still retaining a solid seal against the boiler. I took the boiler out, backed the 90 degree connection out and found the very compressed remnants of a green rubber washer. I dug through the tool chest and found one to match the size and add hopefully enough resistance to allow a firm seal with the boiler and the correct angle to connect to the group head. It tightened down perfectly and I connected the group head connection and started adding the additional connecting pipes for the water level gauge, pressure gauge, etc...

The water pump and motor assembly easily dropped into their position next and I secured the 4 rubber cushioned feet of the motor to the frame with the easily identifiable baggie labeled "pump motor mount hardware." I was able to reuse the stainless steel braided hoses, and I connected them to the main inlet connection and the water inlet tap. I snapped some pictures, but quickly realized after reviewing the deconstruction photos that I had them reversed. I swapped them out and all was well.

It was only a matter of minutes before I realized that I was out of copper pipes and that everything on the hydraulic end of things had been put back together. It was almost anti-climatic. I checked and double checked each nut and snugged them tight and decided to call it a day. The last thing left was to install the electrical parts, connect the solenoid plugs, and rewire the power switch box. I still needed to clean up the exterior panels, drip tray and cup trays, but the functional reassembly was nearing completion.

All in all, I think I had this put back together in about 2 hours. I've spent more time on Scandinavian furniture assembly, but it wasn't nearly as fun.

Wednesday, June 22, 2011

Steam Punk, Milk Funk

The front upper cowl of the machine housed the steam knobs, steam wands, and hot water dispenser in addition to the (limited) electronics for the control pads. This had been set to the wayside while tackling the core of the machine, and at this point it was time to give it some attention.

The first thing I noticed was the missing steam wand from the right side. Upon closer inspection, it had been broken off at the ball joint (shown below). A quick parts search and $67 later, I had a new stainless steel wand with a no-burn elbow for repositioning en route. Not sure why, but it appears the left group head gets more attention on these machines and the steam wand gets more use on the right. I'm sure the equipment setup would dictate a lot of which side is easier to pull from and which side is easier to steam milk. If you had the staff, I'm sure both could be done in tandem; as I know for a fact, that beast of a boiler would give you all the hot water and steam you could possibly need with both barrels blasting. Anyway, I made a mental not that upon reassembly, I was going to install it on the left hand side. It was pretty and I wanted to show it off.

The second thing I noticed was the funk and grime that was built up on the underside of the cover and the near total obstruction of the screen for the hot water dispenser with calcium deposits and crud. It wouldn't be until I took apart the steam valves and wands that I would discover the fossilized milk crud that was subdividing apartments in the steam wand ghetto.





It was gross, but at least it was solid and crusty and didn't provide an odor. I disassembled the steam valves and the hot water valve and started snapping pictures so I would be sure to put the parts back together correctly. I still had the citric acid bath I used for the group heads (from hell) so after dis-assembly, I soaked the parts for 10-15 minutes and then scrubbed them with the brass brush. I left the copper and brass in for a bit longer, but I wanted to get the chromed parts out so the acid would clean, but not damage them. The hot water valve looked almost brand new. The before and after photo of the previously crud filled steam valve was also impressive.











There wasn't much to clean on the electronics, and to my dismay there was a chip out of the corner of one of the control pad frames, but for the price of a new one, I was willing to live with some aesthetic degradation. I scrubbed the stainless cowl with some water and Simple Green to remove as much grime and dirt as possible and then gave it the Macguires Step 1 car polish routine I had given the other high gloss stainless parts. It turned out looking nice, but the quick barista-wipe-down-job-around-the-knobs swirls were still there, and like the control panel, I'm willing to live with the "lived in look" of the machine over paying a fabrication shop to electroplate the stainless to bring it back to a flawless mirror shine.
Before
After

















I reassembled the parts onto the cowl and then set it aside until I was ready to install it over the group heads on the frame. At this point, I have soaked, scrubbed, cleaned, and polished all the parts of the machine. The frame is primed, painted and reassembled, and it's time to put this beast back together. Wait patiently (amidst diaper changes, gardening, and home canning) for the next chapter: Easier to Assemble Than an IKEA Bookshelf.